One of the regular sections of SWZ Maritime is MARS Reports, from the Marine Accident Reporting Scheme. As we receive more of these reports than we can publish in our magazine, we post the other ones online. Read the MARS Report No. 236 here.
MARS Reports cover all kinds of maritime incidents such as (near) collisions and groundings to accidents with tools, falling objects injuring crew and accidents with rescue boats. SWZ Maritime strongly believes relaying these incidents may help prevent new accidents from happening.
Arm Fractured when Rigging Pilot Ladder: MARS 201229
A large inbound vessel was approaching the pilot station in a gale and heavy rain and was instructed to prepare combination ladders on both sides. The C/O and deck crew held a toolbox meeting and prepared the port (weather) side combination ladder first. The gangway was rigged at deck level, and then lowered to the proper height. Next, a seaman wearing all appropriate PPE, including an inflatable life vest and safety harness with lifeline, descended to the bottom platform of the gangway to monitor the lowering of the pilot ladder. After confirming the pilot ladder was 1.5 metres above the water, he began to secure the pilot ladder to two sunken cleats in the hull with an 8mm rope lashing.
When he inserted his right hand into the after sunken cleat to thread the rope through it, a wave caught the bottom of the pilot ladder and jerked it astern. The step in the way of the sunken cleat moved aft and hit the seaman’s right wrist, whilst his hand was still inside the recess. Although in severe pain, he managed to return to the accommodation where first aid was given by the ship’s medical officer. Immediately after berthing, the injured crew was sent ashore and the doctor diagnosed a bone fracture (right ulna), ligament injury and subcutaneous haematoma.
The crewmember was certified unfit for duty and was disembarked.
Seaman securing pilot ladder to sunken cleats
Root Cause / Contributory Factors
- Although a proper risk assessment and toolbox meeting was conducted before work, it did not consider the possibility and consequences of the bottom steps of the ladder being hit by a swell wave.
- A combination of wind direction, restricted sea room, traffic density and routeing prevented a change of heading to provide sufficient lee for rigging the combination ladders.
- Constraints of the working area – in order to secure the pilot ladder to the sunken cleats, the crewmember had to stand on the bottom step of the gangway and pass the lashing rope around both the pilot ladder’s side ropes and twice around the far cleat before tying it off.
Reconstruction of incident showing how the step impacted on seaman’s arm.
Corrective / Preventative Actions
Pilot combination ladder rigging procedures revised as follows:
- Gangway to be lowered to designed level (≤ 55ー angle above horizontal).
- Pilot ladder rope lashing changed from 8mm to 16mm since the larger rope requires only one turn around the ladder and cleat.
- The fore side of the pilot ladder to be lashed fifirst and then the aft side.
- During rigging and unrigging operation, the pilot ladder’s bottom steps shall be kept at least 4 metres above the sea level by means of the recovery line.
- Pilot ladder marked to indicate at upper deck one, two and three metre clearances from ladder bottom to sea level for both ballast and laden conditions.
View of combination ladder arrangement.
Editor’s note: If the pilot transfer craft has sufficient freeboard, under rough sea conditions and with the pilot’s agreement, it would be safer to keep the bottom of the ladder higher than 1.5 metres above the water. Instead of rope lashings that need to be passed around the ropes and cleats and tied off, ‘karabiner’ type quick-release hooks or shackles with a short rope grommet or sling will be more practical, allowing the crew to simply wrap the rope around the ladder and clip the hook either on to its own rope or on to the sunken cleat.
For safety reasons, some pilotage authorities do not permit the use of recovery or tripping lines at the bottom of pilot ladders. Where permitted, the ship’s crew must ensure that this line is led well clear of the ladder and away from the gangway section of a combination arrangement, and kept under adequate tension so that it does not snag or foul the hull of the pilot boat or launch.
Unsafe Operations at Offshore Tanker Loading Berth: MARS 201230
Our crude oil tanker arrived at her offshore loading terminal but due to prevailing severe gale conditions, the vessel remained at anchorage, waiting for the weather to improve. Two days later, an attempt to berth was aborted halfway through as the wind suddenly increased, and the vessel re-anchored. On the morning of the fourth day, the weather improved with a moderate westerly wind. The vessel approached the single point mooring (SPM) to pick up the chafing chain from the buoy and secure it to her bow chain stopper. At that time, the Mooring Master informed the Master that the SPM had been lying unused for nearly a year.
The mooring equipment of the SPM consisted of a chafing chain (76 mm diameter) joined to a polypropylene hawser (80 mm diameter). This connection included a one metre-long weak link comprising of a large oval master link, a Baldt hinged link and a pear link. The weak link had a ‘D’ shackle at each end, one passing through the eye of the hawser and the other passing through the first link of the chafe chain. The purpose of the weak link is to reduce the risk of the hawser parting when picking up/casting off the chain, which has an attendant hazard of whiplash.
During the mooring operation, the Master was attending on the bridge, assisted by the 3/O and one helmsman, while the C/O, the Bosun and two ABs, coordinated by the Mooring Master, were at the forward mooring station. The vessel’s bow had two mooring chain stoppers: one port and one starboard. Both required the hauling line to be led sharply around a pedestal fairlead roller to the winch drum.
No tugs were available for assistance, and on the final approach heading, the vessel started rolling heavily due to the sea and swell on her beam. While the mooring operation was in progress forward, the remaining deck crew swung out the deck crane and began hoisting the cargo hose clamps from the mooring boat. However, due to the beam swell, the crane hook began to swing wildly as no steadying lines had been attached to it. The suspended equipment, including the heavy steel clamps, repeatedly banged on the shell plating. Once clear of the upper deck railings, the load on the crane hook continued to swing dangerously and was impacting heavily on fittings around the manifold area, endangering the vessel and the attending personnel.
After almost a day’s loading, the sea state deteriorated and for safety, the Mooring Master advised the vessel to disconnect the chafe chain and evacuate the berth. Accordingly, cargo loading was suspended and the cargo hoses were disconnected from the manifolds. In order to avoid possible fouling of the propeller by the floating hoses, the Mooring Master instructed the ship’s crew to keep them temporarily suspended from the crane hook until the chafe chain was released and he had manoeuvred the vessel sideways to clear the SPM.
With the chief mate still busy with the cargo calculations in the cargo office, the emergency unmooring operation was commenced by the Bosun and two ABs in a 25-knot wind. The 3rd mate was on the bridge, assisting the Master and the pumpman was stationed at the manifold, monitoring the cargo hoses still attached to the deck crane hook. The 2nd mate was taking his due rest.
The chafe chain was under high tension and was being held in position by the chain stopper, which was secured with the locking pin.
Due to the very short length of the mooring string, the SPM was very close to the bow. To avoid contact with it, the Mooring Master insisted that instead of using a short kick ahead on the engine, the chafe chain be released by heaving in some slack. Because of the excessive tension caused by the wind, the winch was getting overloaded but the crew did manage to heave in a few centimetres and lift the tongue bar clear.
In this position, the weak link lay exactly on the roller of the pedestal fairlead. Due to the sharp nip around it and the resulting high stress, the inboard pear link parted without warning and the chafe chain together with the outboard end of the broken weak link violently flew out through the chain stopper and fell into the sea. Fortunately, no serious injury resulted among the dangerously exposed crew, except for a small piece of rust that embedded itself in the Bosun’s face, just above the left eye. The bridge was informed and while the other crew attended to the wound and removed the rust particle, the vessel now started slowly moving astern, away from the SPM.
Meanwhile, the disconnected cargo hoses were still suspended from the deck crane hook and were temporarily lashed to the hose saddles at the side railings. The sudden astern movement caused these lashings to part and the bights of the hoses fell into the sea. Reacting quickly, the
Master gave a short kick ahead on the engine, and the cargo hoses were unhooked from the crane and safely lowered into the sea.
After re-mooring, the SPM mooring string’s weak link was temporarily removed, inspected and also found to be worn beyond safe limit.
Root Cause / Contributory Factors
- System deficiency – the company did not have detailed procedures for conducting SPM operations, particularly specifying operating environment and tug assistance criteria.
- Exposed location of SPM.
- Possible inappropriate heading on final approach.
- Lack of steadying lines on crane hook.
- Unplanned and hasty disconnection of mooring in strong wind.
- Insufficient manpower on bow and manifold area.
- Poor communications between Mooring Master, ship’s Master and deck teams.
- Absence of tug assistance.
- Ineffective maintenance of terminal’s mooring system – excessive wear on small pear link of the weak link which was not noticed or rectified by the terminal operator.
- Sharp nip in the hauling part of the chafe chain at the deck pedestal roller.
- Failure to lower the cargo hoses into the water before releasing mooring.
- Failure to use engine to ease tension on chafe chain.
Illustration of mooring arrangement before commencing heaving on the hawser – note the sharp nip around the pedestal roller.
Corrective / Preventative Actions
- Company procedures amended to include a new risk assessment before commencing SPM operations. The risk assessment requires the Master to ensure:
– Evidence of Mooring Master’s competence/experience and certificate of test and periodic maintenance of the SPM equipment related to the mooring assembly (hawser-chafe chain- weak link).
– If the Mooring Master is not able to provide any of the above documents, the Master must carry out an assessment of the real status and condition of the mooring equipment beforecommencing mooring operation. Company DPA to be informed accordingly
– Personnel attending at the bow station must be properly briefed before the operation and must be familiar with the hazards and limits of snap back zones.
– An experienced and responsible deck officer shall be in charge of the forward station when connecting/disconnecting chafe chain.
– Ship’s Master shall not entirely depend on the Mooring Master’s skill and shall actively take over the con in order to ensure safety of personnel, equipment and vessel. - A fleet circular was sent to the fleet describing the incident and lessons learned.
- A report of the incident was forwarded to Intertanko with the recommendation that the terminal operator ensure the proper
integrity and operational condition of the SPM equipment. - Incident shared with the industry to avoid similar recurrence.
- All fleet Masters instructed to closely monitor the condition of every SPM and associated mooring equipment and submit reports to the office on the real status of the SPM equipment at offshore terminals.
Illustration of mooring arrangement after the hawser was heaved in with the weak link sharply nipped on the pedestal roller. The pear link parted at this point.
Editor’s note: Appendix E.4 of OCIMF’s publication Recommendations for Equipment Employed in the Bow Mooring of Conventional Tankers at Single Point Moorings (4th Edition, 2007) recommends that ships delivered before 2009 should be equipped to safely handle pick-up ropes taking into consideration safety and protection from risk of whiplash injury to mooring personnel. Additionally, on ships delivered after 2009, it is recommended that pedestal roller(s), if fitted, shall not exceed two in number and should be correctly positioned to enable a direct lead from the centre of the bow fairlead to the centre of the bow chain stopper. The angle of change of direction of the pick-up rope lead should be minimal. On this tanker, it would appear that the change in lead angle around the pedestal roller was excessive.
Additionally, managers must ensure that the latest local marine weather synopsis, isobaric charts and forecasts are available to the vessel, especially in regions where weather conditions may be prone to rapid changes or the SafetyNet service coverage may be less than optimum. In this incident, such data would have assisted the ship’s command in better decision-making and could have potentially averted the aborted and hazardous mooring and unmooring operations.
Acknowledgement
Through the kind intermediary of The Nautical Institute we gratefully acknowledge sponsorship provided by:
American Bureau of Shipping, AR Brink & Associates, Britannia P&I Club, Cargill, Class NK, Consult ISM, DNV, Gard, International Institute of Marine Surveying, Lairdside Maritime Centre, London Offshore Consultants, Lloyd’s Register-Fairplay Safety at Sea International, MOL Tankship Management (Europe) Ltd, Noble Denton, North of England P&I Club, Port of Tyne, Sail Training International, Shipowners Club, The Marine Society and Sea Cadets, The Swedish Club, UK Hydrographic Office, UK P&I Club
Submit a MARS Report
More reports are needed to keep the scheme interesting and informative. All reports are read only by the MARS-coordinator and are treated in the strictest confidence. To submit a report please use the MARS report form (MARS@nautinst.org)